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Stock
Join Date: Feb 2012
Location: Kansas
Posts: 8
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So I decided to blow some of the cobwebs out of my mk3 the other day and right before I shifted to 3rd (around 5600-5700rpm and pushing 9 psi, fyi...i have a stock turbo and my EVC was set to override the OEM settings) the engine cut out/stopped boosting, but the car did not die and the check engine light came on momentarily. It felt like i over boosted and the car shut down to keep the engine from "exploding"?
The only things i noticed are that there is no longer the wastegate flutter when i shift/let off throttle. And after i shift there seems to be more turbo lag than usual. It is boosting though, cause the needle does go over 0 psi and i can hear it. It also doesn't seem to pull like it used to. I have spent several hours tinkering with the actuator, o2 sensor, bov, etc. really trying to avoid taking the turbo and/or down pipe off and really want to avoid taking it to a shop. I also reset the EVC (HKS evc III) which was probably a bad idea since the car wasn't boosting properly? I know next to nothing about this stuff and i looked at similar forums on here but i couldn't find any solutions. Any suggestions would be appreciated ![]() |
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Thread | Thread Starter | Forum | Replies | Last Post |
Wastegate? | Austinw88 | MKIII Supra | 7 | 06-21-2011 01:59 AM |
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Boost Issues | abhattan | MKIII Supra | 1 | 04-25-2007 02:57 AM |
External Wastegate! | teedoff00 | MKIII Supra | 1 | 04-11-2007 03:49 AM |
Wastegate? | drmmr15 | MKIII Supra | 19 | 01-16-2007 07:07 PM |